<center id="61a5n"><menu id="61a5n"></menu></center>

      首頁 > 新聞資訊 > 行業新聞 >

      鍋爐低氮燃燒器改造后低負荷汽溫無法達設計值

      時間:2018-07-11 10:54    作者:admin 返回列表


      1、設備簡介
      1.equipment introduction

      某廠SG1025/17.4-M847型鍋爐為上海鍋爐廠制造亞臨界、一次中間再熱、自然循環、固態排渣爐,鍋爐為∏型布置,采用平衡通風,四角切向燃燒,配四臺低速鋼球磨中儲式制粉系統。設計煤種為貧瘦煤。鍋爐50%額定負荷滑壓工況下設計過熱汽溫540,再熱汽溫515℃。
      SG1025/17.4 M847 type boiler at a factory for manufacturing subcritical boiler plant in Shanghai, a reheat, natural circulation, solid-state slag furnace, boiler of ∏ type is decorated, USES the balanced ventilation, tangential firing, with four reservoir type in low speed ball mill coal pulverizing system. Design coal for zhengzhou area lean coal. 50% rated load sliding pressure boiler design superheated steam temperature of 540, under the condition of reheat steam temperature 515 ℃.

      主燃燒器一次風及二次風逆時針方向布置,雙切圓直徑大小為719/?686。三次風順時針方向布置,與一、二次風方向主軸反偏10度。SOFA燃燒器順時針方向布置,與一、二次風方向主軸反偏6度。三次風與SOFA風共同起消旋風作用。
      The primary and secondary air of the main burner are arranged counterclockwise. 719 /? 686. Three times the wind clockwise direction layout, with one, two times the wind direction of the main axis back 10 degrees. SOFA burner is arranged in a clockwise direction, 6 degrees backward from the main axis in the direction of first and second wind. Three times wind and SOFA wind together play the role of anti - cyclone.

      主燃燒器一、二次風噴口與SOFA燃燒器噴口均裝有自動垂直擺動裝置。一、二次風噴口可上下擺動±30度,擺動機構分為上、下兩組。SOFA風噴口還可以以手動方式左右擺動±15度。

      Both the primary and secondary air vents and the SOFA burner vents are equipped with automatic vertical swing devices. First, the secondary air nozzle can swing up and down plus or minus 30 degrees, the swinging mechanism is divided into upper and lower groups. SOFA air nozzle can also swing from left to right in manual mode, plus or minus 15 degrees.

      低氮燃燒器


      2、1#機組150MW低負荷工況下的汽溫問題及原因分析
      2.Analysis of steam temperature problem and its causes in 150MW low load condition of unit 21

      鍋爐低氮燃燒器改造后主要存在單套制粉運行時主汽溫度、再熱汽溫度低,但后屏過熱器管壁超溫,一級減溫水量增加的現象。通過試驗發現當在150MW時如果投運兩套制粉系統,如A、C或B、C制粉系統汽溫可以達到536℃~538℃,且后屏不超溫,過熱器有減溫水。當投單套制粉系統,過熱汽溫最低時達504℃左右,再熱汽溫低達495℃左右,但是過熱器一級減溫水量卻達到近40t/h,前屏也經常超溫。
      The main steam temperature and reheat steam temperature of a single set of pulverized powder are low after the modification of the boiler low nitrogen burner. Through the study found that when in 150 mw if put two bearing powder system, such as A, C or B and C pulverizing system steam temperature can reach 536 ℃ ~ 538 ℃, and the screen is not overtemperature, superheater with warm water. When single bearing powder system, superheated steam temperature when a minimum of 504 ℃ or so, low reheat steam temperature of 495 ℃ or so, but the superheater level of desuperheating water flow to nearly 40 t/h, front panel also often overtemperature.

      分析單套制粉系統運行過、再熱汽溫偏低原因為:
      The reasons for the low reheat steam temperature of the single set pulverized powder system are as follows:

      (1)當投運兩臺磨時,燃燒器四角能夠兩兩相對投運三次風,作為反切消旋功能的三次風流場相對均勻,爐膛出口煙氣流場偏差較小,屏底超溫較好。
      (1) when the operation of two grinding, the corners of the burner to three times the wind two relative was put into operation, the methods of three wind field despun function is relatively uniform, furnace exit deviation is small, smoke flow in the bottom of the screen overtemperature is better.

      (2)當投運單臺磨時,燃燒器四角只能夠投運一個對角三次風而無法形成有效的消旋流場,再者對角三次風的氣固兩相流速可能不均勻而有可能導致流場的紊亂,使得爐膛出口煙氣流場偏差增加,引發屏底超溫,過熱器減溫水大量增加,屏后煙溫降低,限制了過熱汽溫及再熱汽溫增加。
      (2) when cast waybill grinding machine, three times in the corners of the burner can only put a diagonal wind to form effective despun flow field, moreover diagonal three times the wind of the gas-solid two phase flow rate may be uneven and could lead to disorder, the flow field in the furnace exit deviation of smoke flow in increasing, lead to the bottom of the screen overtemperature, superheater reduction with warm water, screen after smoking temperature is reduced, limits the superheated steam temperature and reheat steam temperature increase.

      (3)相對于投運兩臺磨,單臺磨投運時燃燼區煤粉濃度低于兩臺磨投運時的工況,屏底煙氣溫度也相應較低。
      (3) compared with the two mills, the coal powder concentration in the embers area in the single mill is lower than that in the two mills, and the flue gas temperature at the bottom of the screen is lower.

      3、治理方案及效果
      3. Governance scheme and effect

      針對低負荷單套制粉系統主、再熱汽溫偏低問題原因,提出以下治理措施:
      In order to solve the problem of low main and reheat steam temperature of low-load single set pulverized powder system, the following measures are proposed:

      (1)提高爐膛送風量,可提高煙氣流量。
      (1) to increase the air flow in the furnace can increase the smoke flow.

      (2)調整SOFA風左右擺角,中、下層SOFA風已經調成與一次風及二次風一致,均為逆時針方向布置,上層SOFA風與一次風及二次風反切。配合主燃燒器消旋二次風及其它二次風比例以控制爐膛出口煙氣溫度及煙氣量的偏差,控制屏過金屬溫度兩側無偏差時盡量減少減溫水量提高汽溫。
      (2) adjust the left and right Angle of SOFA wind, and the middle and lower SOFA wind has been adjusted to be consistent with primary and secondary wind, both of which are arranged counterclockwise. The upper SOFA wind is opposite to primary and secondary wind. Cooperate with the main burner despun secondary air and other secondary air ratio of air to control the furnace exit flue gas temperature and smoke deviation, control panel metal temperature without deviation on both sides to minimize desuperheating water flow to improve the steam temperature.

      (3)在以上基礎上汽溫仍低時,采用調節主燃燒器擺角向上;適當啟動部分D層燃燒器;減少磨機再循環率,提高三次風量;盡量提高C、D層給粉機轉速,降低A或B層給粉機轉速等方式亦可提高汽溫。
      (3) when the temperature of the above foundation is still low, the swing Angle of the main burner is adjusted upwards; Properly start part D layer burner; Reduce the recirculation rate of the mill and increase the air volume three times. The steam temperature can be increased by increasing the speed of layer C and layer D feeder as much as possible, and decreasing the speed of layer A or layer B feeder.


      上一篇:低氮燃燒器改造后穩定燃燒分析 下一篇:低氮燃燒器選擇考慮的主要參數你知道嗎?

      Copyright ? 2018 北京眾誠永源節能環保技術有限公司 專注于低氮燃燒器設計、改造、銷售和安裝。網站地圖   備案號:京ICP備10001485號-1

      北京網站建設藍杉互動
      超碰在线免费

        <center id="61a5n"><menu id="61a5n"></menu></center>

          国产精品一|国产精品点击进入|国产精品无码免费播放|国产精品扒开腿做爽爽的视频| 香蕉大伊AV|香蕉视频一区二区三区|香蕉久久人人爽人人爽人人片av|99精品国产一区二区香蕉| 91免费在线|91国内精品线免费播放|91国内精品久久人妻无码大片|91久久精品美女高潮喷水白浆| 91 免费国产永久入口|91 免费 无码 国产在线播放|91偷拍一区二区三区精品|91久久精品美女高潮喷水| 中文字幕二区|中文天堂在线一区|中文无码久久精品高潮喷水|中文字幕精品久久久久人妻宅男| 亚洲一区在线|亚洲乱熟女一区二区三区|亚洲一区二区自偷自拍另类|亚洲AV无码精品一区二区久久| 亚洲剧情中文字幕影院,亚洲十八 精品网站污污污,亚洲午夜久久久久中文字幕久,亚洲午夜无码久久久久| 亚洲国产精品无码|亚洲国产91精品无码专区|亚洲国产精品无码久久九九|亚洲中文字幕最新2021芒果| 国产精品99|国产精品久久久久久免费字体|国产精品偷伦一区二区|国产精品ⅴa无码一区二区免费看| 亚洲国产精品视频|亚洲精品在线观看|亚洲精品无码永久中文字幕|亚洲精品无码久久久久久久| 久久黄色网站,久久这里有精品,久久高潮一级毛片免费看,久久精品国产99精品国产亚洲性色| 在线中文字幕|中文字幕在线观看|最近最新中文字幕高清免费|最近中文字幕高清中文字幕网| 九九精品|嫩草91亚洲精品|自拍偷自拍亚洲精品熟妇人|山外人精品影院| 久久久久人妻一区精品色|久久久久久人妻精品无码|久久久久久精品无码人妻|久久久久久精品人妻免费网站不卡| 亚洲国产精品视频|亚洲精品在线观看|亚洲精品无码永久中文字幕|亚洲精品无码久久久久久久| 亚洲国产精品无码|亚洲国产91精品无码专区|亚洲国产精品无码久久九九|亚洲中文字幕最新2021芒果k9f752 精品国产国偷自产在观看|精品少妇人妻AV无码久久|精品无码久久久久久久久网站|精品国产91久久久久久浪潮|nzr287 色色综合|色五月婷婷|色婷婷国产精品视频一区二区|色婷婷AV一区二区三区麻豆9lp615 国产免国产免费|国产精品久久久久久久|国产精品久久久久久无码专区|国产一级无码AV免费久久1|srt244 91免费 无码 国产在线观看|91性高湖久久久久久久久|91国内精品人妻无码久久久|91免费精品国自产拍在线观看|gl9747 人妻久久久一区二区三区,人妻少妇看A偷人无码精品,人妻少妇精品视频一区二区,人妻无码久久久久久久久久久kyt260 91在线视频播放|91水白嫩网站 喷水|91免费 无码 国产在线观看|91精品久久久久久久久中文字幕|m9x508 91精品免费久久久久久久久|91精品国产91久久久久久手机|91精品国久久久久久无码|91色老99久久九九爱精品|iki330 亚洲一级AV|亚洲AV乱码一区二区三|亚洲AV无码一区二区三区性色|亚洲AV综合色区无码一二三区9dt408 国产无码精品|国产精品久久久久久久精品三级|国产精品久久国产精无码|国产特级毛片AAAAAA高潮流水hii210 精品亚洲国产91在线|精品丝袜人妻久久久久久|精品中文无码少妇Av毛片免费|精品久久久久久中文字幕无码一区|0hu976 人人妻人人澡人人爽一区,人妻人人做人碰人人爽91,人妻久久久久无码中文字幕,人妻精品久久久a无码专区色视|lv0987 91色国产在线|91麻豆精品国产91久久久久久|91精品国产91久久久无码|91精品国产91久久久久水蜜桃tos356 精品无码|精品三级久久久久久久电影|精品久久久久久精品中文字幕无码|精品久久久久久亚洲偷窥很黄很污f8q477 精品国产无码|精品性高朝久久久久久久|精品无码人妻一区二区三区18|精品国产91久久久无码JDANbki475 奇米久久|奇米影视亚洲春色|奇米影视7777久久精品人人爽|奇米精品一区二区三区在线观看8vr715 91精品国产|91精品久久久老熟女91精品|91精品久久久久久久久无码|91精品久久久无码中文字幕vrhea214